After the purchase, the TA’s gearbox turned out to be defective. 2 teeth were missing from the 2nd gear. Later I (fortunately) discovered both teeth in the gearbox’s oil sump.
This second gear is the most vulnerable gear, especially because people often try to drag a TA in 2nd gear.
Or they try to get the engine loose by force dragging it in 2nd gear.
Fortunately I was able to buy a NOS gear via the TA club warehouse and after an evening of reading the garage manual I dismantled and reassembled it.
Easy to do most of this myself. With help from my brother in his garage, to set the Timken bearings at the correct tension and adjust the play of the differential.
After converting my Traction Avant to 4-speed, I noticed that the car’s braking power is only just sufficient to drive safely in today’s traffic.
Unless you firmly press the brake pedal; then something does happen!
Especially with several passengers in the car the braking power seems to be on the small side, probably because we are used to power brakes in modern(er) cars.
Kicking harder on the brake pedal also helps, and the well adjusted new brake linings on the brake drums make sure that the car will block on all wheels in case of a panic stop.
Nevertheless, I started looking for possibilities to mount disc brakes on the front wheels.
In France, until 2004, there was a manufacturer that sold kits with discs, caliper adapters and calipers.
Without a brake booster but that is certainly not a big problem, a 7 inch brake assist booster (aftermarket add-on) fits from any ’60-’65 kit . So this might be the next project:
Did call and email but never got in touch….
Still going to make it myself!
Or just place a brake booster in combination with a suitable master cylinder, then I can use the existing drum brakes and make 2 separate circuits.
With an ordinary soldering torch you can solder aluminum with special rods, at a much lower temperature than when you can weld aluminum. If you clean the materials with a stainless steel brush and preheat the materials well on, for example, a 4-burner stove, you can solder aluminum with an ordinary soldering torch (for tin). I managed it and it is absolutely hard and tight!
Sometime around 2006/2007 I initially fitted the Traction Avant with a CTA 6 volt alternator.
Above you see the CTA kit that I originally used to convert the 6 Volt system from DC to AC. You can also see the alternator from CTA installed at the time, the bracket from CTA never really worked well and seemed to be on the weak side.
Shortly after that I converted the car to 12 Volts.
I then replaced the regulator from the 6Volt type to a 12 Volt separate regulator.
That never really worked well. The charging current seemed reasonable but the voltage never rose above 12.4 Volts.
While a full battery when charged is at about 13.4 Volts.
After a lot of research and searching, I put a fixed regulator on the alternator, but that didn’t help either.
Now it seems that the field winding just can’t handle more because this alternator is wound for 6 Volts.
Seems strange to me, if you turn faster you get more voltage according to the Faraday book, but there also seems to be a saturation of the ironwork.
Later again, I converted the Traction to a 4-speed, with an ID19P engine and corresponding drive pulley for the water pump and alternator.
So in the end I just bought a new 12 (14) Volt alternator from ISKRA, actually a Mahle one.
This alternator delivers 14 Volt max and 33 Ampere max.
It still needed some modifications, of course a new bracket…
And the pulley had to be moved a little on the shaft.
I moved the big ring on the outside to the inside, behind the pulley and with that the offset was sufficient.
I found the bracket of the CTA set-up too weak, I had already replaced it for a sturdier home-made type.
The ISKRA alternator fits exactly in this bracket and further connection is no problem at all.
I have already converted my pulleys to thin belt dimensions of 10 mm because I was stuck to the pulley of the ID19P, which I wanted to keep because it is a bit larger than that of the original Traction Avant. This makes the water pump run just 5% faster and that seemed a good idea in connection with possible extra heat development from the ID19P engine, it was of course also the original pulley from that type of engine and it all just fitted with the engine mounting in the Traction Avant…
It remains to be seen, because the water pump of the TA is slightly different than that of the iD19P. It all works fine though.
The new alternator also works perfectly and charges the battery at 13.4 Volts.
In the end I did some calculations on the RPM’s you need to get a good charge.
From the graphs of this ISKRA alternator you can see that it only does something above 1200 RPM up to 7500 RPM.
The ID engine makes 650 RMM at idle up to max 3800 RPM.
The camshaft turns half the speed of the crankshaft so 325-1900 RPM.
The camshaft pulley of the ID19P is 21cm in diameter and that of the Dynamo is 7cm in diameter, this gives an acceleration of exactly 3x.
The shaft rotation speed of the dynamo is therefore between 975 and 4700 RPM. That’s too little to charge anything at idle.
The pulley of an old DS20 alternator was turned from double pulley to single pulley by me earlier and was mounted on the CTA 6V alternator, see the photo higher in this article. This one has a diameter of 6cm. The acceleration from crankshaft pulley to dynamo is then 21/6=3.5x.
With this smaller dynamo pulley, the shaft rotation speed of the dynamo becomes 3.5 x(325-1900) RPM, so 1150-5650 RPM. That’s just enough to charge something at idle.
See below an action picture of the moving fan and pulley c.q. belt….
Switched DC-DC proportional inverters have been made and installed for all motors such as windshield wiper and heater. The bulbs have all been replaced for 12 Volt types and the signal driver has also been replaced. The fuel gauge ballast resistor has been modified, the air horn pump, and the starter motor have all been replaced for a 12 Volt type. Control lights, dash lights and so on have all been replaced as well. And… just a bit more about how it was with the DC alternator:
The Traction Avant is regularly parked at our place for long periods of time.
Each time, the level of my brake fluid when I picked up the car was at minimum, while I had put the car away with maximum level.
The reason turned out to be that on almost all parts where the original meager mineral brake fluid could flow under gravity along a brake cup, it actually did.
The result was a lot of filth and an empty reservoir.
The residual pressure that keeps the rubbers sealing nicely, drops off after a certain time and then this above mentioned problem arises.
The solution turned out to be upgrading to DOT3 brake fluid. DOT 3 has somewhat lubricating properties which in my experience keeps the seal between cylinder walls and brake cups closed.
I’ve been using it this way since 2015 and haven’t lost a drop of DOT3 since.
An additional advantage is that because of the lubricating effect the brake pistons no longer get stuck as a result of the long downtime during the winter, in combination with the hygroscopic effect of the old brake fluid.
It was quite a job to get the old fluid out completely, flushing with methylated spirits, blowing crosswise until all the methylated spirits were removed at each end point.
Then fill up with DOT3 and do some serious bleeding.
DOT 4 is not a good idea in any case, at least not with the original rubbers.
The additives in DOT4 cause the original rubbers to swell. If you want to use DOT4 or any other DOT version than DOT3, replace all rubbers and cups of the wheel brake and master cylinder with after market (so do NOT use old stock) rubbers and cups.
Good luck!
Update 3-2021: Everything is still fine with the brakes, I did remove the front brake cylinders as a precaution, cleaned them completely, flushed them out and filled them again with new DOT3.